Tubing water shutoff solution improves productivity
The RELAY™ Digital Slickline helped an operator, located in Algeria, increase oil production and reduce water cut by 21% and improve well productivity.
Case Study
Operator controls major loss event in Gulf of Mexico
Halliburton's BaraBlend®-680 lost circulation material helped salvage the well, reduce losses, and move to the production zone while saving over USD $1M.
Data Sheet
MRIL®-Nuclear Magnetic Resonance - Data Sheet
Veto™ 3 Subsea Safety Tree - Data Sheet
Case Study
RapidStage system with AccessFrac service in the Bakken
RapidStage system using Swellpacker isolation system - two discrete fracture treatments in a stage can be achieved by introducing AccessFrac in Williston Basin.
Case Study
Santos adopts engineered solution to avoid stuck pipe incident
Customized drilling fluid increases ROP, saving 1.5 hours of rig time per vertical well, reduces safety exposure, and lowers well cost by USD 600,000.
Case Study
Wellbore cleanout saves customer in Angola 18 Million USD
Halliburton operation helps a customer avoid 90 days of deferred production and a coiled-tubing intervention and saves USD 18 million in Malongo, Angola.